In view of my deterioration in health nothing further has happend to the MX3 until yesterday. I decided that having bought all the parts for the outstanding work on both cars I should bite the bullet and ask my mate and former business partner to come and do the work for me as a paid job.
The parts I had assembled were:
MX3 all new parts:
Alternator
Water pump
Timing belt kit with tensioners
Air filter
Oil filter
Fuel filter
Coolant
Engine oil
Subaru
Oil filter
Engine oil
(I had completed the rest of its service before I got sick)
So yesterday my mate arrived at 09.00 and after a quick coffee we set about jump starting the MX3 and getting it onto the ramps on the drive. That meant SWMBO had to get her car out and she accepted that it may not be back in on the same day!!

- As it is now with o/s front wheel and ramp in temp place for extra safety while waiting. Car actually supported on the axle stands.
Well it hasn't gone back yet due to three seperate problems that arose during the work, firstly the alternator charging stud is 13mm where the original had been 10mm so the spade terminal on the charging lead will not fit. Of course sods law dictated that I had 7 different sizes in stock but no 13mm - one order to Amazon for delivery today.

- The new alternator

- The spade that was too small

- The new spade to be crimped onto the lead
Secondly the timing belt kit I had turned out to be wrong, which we hadn't opened until the strip down was complete! I had triple checked the compatibility on the website before ordering so when it arrived back in April I simply put it on the shelf to use when I recovered. On looking at the kit it had Gates part number K015273XS where as the correct one is part number K015274XS so I assume it was a picking error on their side!! I spent an hour trying to track down the correct one to collect and use yesterday but to no avail. The best I could do was one for me to collect today, which I have now done.

- Wrong part number

- Wrong kit

- Correct part no

- Correct kit
Thirdly having had to stop work on the timing Dave set about the rest of the service work, replacing the filters, oil change and install new water pump, which is where it all went wrong again!! The metal water bypass pipe connecting the heater return back to the water pump had corroded to the point of not being resealable with the push fit O ring seal as designed. I am currently looking for a complete replacement pipe but so far I have only found a similar one from the MX5 which we may be able to fabricate a replacement end for my pipe from. Watch this space!!

- Water pump

- The wrecked joint (now bodged until proper fix available)
So at that point we realised it wasn't our day and shut the bonnet and the garage door to hide the state of it as in the picture below, note the chair which is where I had to spend 85% of the time only getting up to find something for Dave or make a loo trip!!
Hopefully we will get the job finished on Monday or Tuesday weather permitting but the pipe will be an outstanding job methinks.

- The garage as we have now left it