I've had something of a critical patience failure with the Invacar sitting immobile in the garage. It's getting sorted. Not in six months time, now. Realistically I'm not much closer to a replacement hub than I was in September. A few leads but nothing has yet materialised.
It's been a while, so here's a recap of the current situation.
[] On 2nd September 2019 I went to get a slow puncture on the nearside wheel sorted.
Just needed the rim cleaned up a bit, took five minutes to sort. Right up until this happened.
Closer inspection revealed the rest of the studs on this wheel to also be knackered. You can actually see the upper right one is bent in the photo.
[] Three of the studs unscrewed from the hub without too much protest. Except for the one which had already snapped. Which snapped twice further before ending up snapping totally flush with the hub.
[] At this point I made a blundering mistake. Rather than taking the hub off and sending it to a machinist to be sorted, I figured I'd have a shot at drilling out the remains of it in situ.
This was foolish for a couple of reasons. The first was that I had utterly underestimated how hard to source a replacement hub would be if I could things up. Secondly was that I was doing this folder into a cramped, poorly lit corner of my garage. So there was absolutely zero chance of me drilling it out straight as I couldn't see what I was doing and by the time I had the drill set up had already lost feeling in my left leg. I'd also underestimated quite how awkward this job was determined to be.
By the time the stud was removed the hole was distinctly oval. That is the point at which I started seriously looking for another hub - and that's where we are still.
It took a bit of experimentation, but we managed to figure out that threads in the hub are 3/8" BSF, and there are currently three high tensile bolts holding the wheel on. I'm not 100% happy with the way I've had to use the original wheel nuts (they're bog standard Mini ones) to centre the wheel, I really need to get some proper conical washers.
Having thought about it a bit I don't see any problem using bolts rather than studs and nuts. I can see that they'd use the studs when the cars were in service as it's going to be far quicker to swap out a stud if the threads get mangled than change a hub. However I'm hardly going to have the wheel off every weekend, and with me being careful rather than monkeys in Kwik-Fit it should be absolutely fine.
The remaining one is getting drilled out to the first size necessary to get the hole properly round and is then getting tapped and an appropriately sized bolt will then be fitted. It's not a perfect solution but in the real world it should be absolutely fine. Plenty of cars far heavier and more powerful do just fine with three wheel nuts or bolts just fine...and I really can't see a 400kg 20bhp three wheeler having the slightest issue because the fourth bolt is a fractionally different size. So long as the wheel is properly clamped against the hub it will be just fine. The only issue I can possibly forsee is the balance being thrown off a little if the one bolt is slightly heavier, but realistically I'm not going to be doing hot laps around the 'Ring...it'll be fine. There's enough vibration from the drive and the engine as it is I'm probably not likely to even notice if there's a slight imbalance from a wheel.
This isn't going to be a long term solution. Once the world returns to some semblance of normality I'll be pulling the hub and sending it to a machinist to be sorted out, probably adapted to take standard press-through Mini studs. However as all of the places I'd be looking to send it are currently closed, I'm forced to improvise. Everything will be very carefully monitored but I'm really not expecting issues once the wheel is bolted on.
Plus if the usual way of the universe continues, the moment I get a workaround sorted another hub will materialize as if by magic in tomorrow's post.
Drilling things went okay today, the hole I'd already got wasn't far off round. However then this happened.
Ah. It's going to be one of *those* days is it...
Apparently my tap set is made of cheese. I'll get a hopefully better one ordered and then we'll come back to this.
Meh, plenty of other things I can do today.
First up came under the heading of "unexciting but worthwhile" in that I made a run round both the van with some grease. The passenger door on the Jag has creaked like a prop from a Haunted House since it arrived on fleet. The bonnet has been sticking a bit on the van lately too. So I went round and greased all the door, boot and bonnet hinges, the pivot points for the gas struts and the latches. I didn't realise how badly the bonnet on the Jag was binding before, it now opens and closes silky smooth, no creaking or groaning. The doors on the van now snick closed with the gentlest push as they should.
I do need to adjust the bonnet closure on the Jag a bit, the driver's side rear corner sits a bit too high and bounces around a bit when driving. Slight echoes of the Lada there...though in that case you need to leave a little slack or the cable will snap the first time you pull the release handle...and if that happens you're in for a world of pain getting in. Been there, done that, have the scars to show for it. You really don't want to have to deal with a Lada Riva with a snapped bonnet cable unless you have a spare bonnet on hand and can just take a grinder to it.
Next up I wanted to check the tension on the new belt I'd fitted, it's had a couple of trips out to bed in, seems generally fine but has been giving a brief chirp of protest from the power steering when first backing out of the drive.
Did seem a little loose, so time to nip it up a bit.
The lock nut is moderately awkward.
The adjuster that I needed to wind out to tension things up on the other hand is exceedingly fiddly.
Your arm is wedged between the exhaust manifold heat shield and the inner wing and have a working arc of about 10cm between the exhaust downpipe which limits your space upwards and the top of the power steering reservoir itself which gets in the way downwards. Between each movement you need to rotate the spanner 180 degrees and have a 50% chance of dropping it into the bowels of the engine bay. It's fiddly. No access from above unless I attack the spanner with the grinder as there's a metal coolant line in the way.
Simple enough though, just fiddly. Seems to have sorted the squeak, I'll check it again in a week or two, but it should be fine now I think. Need to go back in to swap the fan belt once the new one shows up anyway.
It was starting to spit with rain at that point, but I wanted to get one more thing ticked off. The rear fog lights weren't fitted properly and were pointing inwards towards each other. Made the back of the car look cross-eyed. It was bugging me.
There are two large washers and a shakeproof washer on the fitting bolt, these had been fitted incorrectly.
Both of the penny washers were below the mounting bracket which was pulling the light down too far.
Instead there should be one on each side of the bracket, like so.
Problem solved.
Looks immeasurably better. Just need to sort the exhaust tips and the back of the car shouldn't look off any more.
The heavens then opened, so that was the end of it for the day really!
We'll have to see what the weekend holds, sure I'll find things to keep me busy.